To: | <[email protected]> |
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Subject: | Re: LF: W1VD amp help - more waveforms |
From: | <[email protected]> |
Date: | Mon, 9 Apr 2018 13:56:14 -0400 |
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PaulOne other quick observation ... the leads of the thick film snubber resistors that go to ground are rather long. It's probably not visible in the photo of mine, but the milled circuit board 'pocket' has the copper ground plane close to the body of the resistor. Try sticking a small piece of circuit board or copper strap in there to make a wide connection to the ground plane. May not matter much ... but we're trying to eliminate all possibile problems. Jay W1VD----- Original Message ----- From: <[email protected]> To: <[email protected]> Sent: Monday, April 09, 2018 1:41 PM Subject: Re: LF: W1VD amp help - more waveforms PaulThanks for the photos and information. I was more interested in the superimposed gate waveforms than the drains, though. A pix of the LPF as well would be appreciated ... think there was one last week. Just for the record ... my doubler was never mounted inside the amplifier ... so you are covering new ground with that. I would think having it external to the amplifier would be less problematic. For testing, stick to driving it with the HP3325A for now ... which is what you're most likely already doing.Can't find much fault with the construction ... other than the somewhat loose primary winding on the transformer. In mine, the primary winding was nestled inbetween the turns of the secondary. This is important to minimize leakage reactance ... which also contributes to excessive ringing.Think I would continue to concentrate on getting the ringing down before going to high power. One other thing ... have you double checked that you have the correct capacitance in the LPF? Jay W1VD----- Original Message ----- From: "N1BUG" <[email protected]>To: <[email protected]> Sent: Monday, April 09, 2018 11:34 AM Subject: Re: LF: W1VD amp help - more waveformsYep, voltage breakdown of the FETs was my worry. However I may be making a false assumption. I assumed the voltage spikes in the ringing would vary linearly with applied drain voltage? Perhaps that isn't necessarily so? With 13V on the drains the first spike here is 'about' 64V. Efficiency seems fine. I wouldn't try to put an exact figure to it what with measurement accuracy in three places (voltage, current, RF power) but it 'appears' to be in the mid 90s. Paul On 04/09/2018 11:02 AM, [email protected] wrote:Alan The main concern about the ringing is that the positive extreme stays below the drain source breakdown voltage ... with some 'headroom'. Otherwise ... Jay W1VD----- Original Message ----- From: "Alan Melia" <[email protected]>To: <[email protected]> Sent: Monday, April 09, 2018 10:21 AM Subject: Re: LF: W1VD amp help - more waveformsPaul I think you need to step back from this a little. One point, design/cable routing at 137kHz isnormally not that critical and it is unlikely it is having much effect. Many us have ''haywired''PAs at these frequencies without major troubles....even using croc-leads!!You are unhappy about the drain waveforms.......why?? the ringing is on the ''off'' device and sodoesnt really matter in terms of efficiency. Consider what is happening. The FET drive goes off and the drain current starts to drop inductance in the drain feed causes the voltage to rise to try to keep the current flowing. Then on top of this the other transistor switches on and the transformer connection for the off side sees a rising induced voltage out of the transformer. There is bound to be overshoot but it does not absorb much power. It may be the generous ''dead zone'' (whilst a good idea) that is producing this picture. The critical part is the the flat zero volt line when the FET is on. The current pulse rings abit, but the current drops in the second half of the pulse.....why?? This, I think, is really theloss of power. Does Jay's show this? The point I am making is don't get drawn up blind alleys because a trace just does not look ''pretty''.I think we have mentioned this before but the transient performance of the power supply may be afactor. There should not be great changes in the current draw because you are switching the PSU load from one transistor to the other but there can be higher speed transients that can affect power supply regulators in unexpected ways.As Andy said efficiency at 12v is not very meaningful because of the high rds of these FETs. It isusefull to run up a PA at low volts say for safety when the antenna needs to be tuned. Finally the scope probes are placing an. albeit small, capacitance across the drains (I am assuming they are correctly trimmed) The waveform can often be affected by where the ground is picked up from. Stick with it because you are close to being ''there'' Alan G3NYK |
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