Return-Path: Received: from post.thorcom.com (post.thorcom.com [195.171.43.25]) by klubnl.pl (8.14.4/8.14.4/Debian-8+deb8u2) with ESMTP id w39HlfmZ022635 for ; Mon, 9 Apr 2018 19:47:43 +0200 Received: from majordom by post.thorcom.com with local (Exim 4.14) id 1f5apL-0003Rn-UI for rs_out_1@blacksheep.org; Mon, 09 Apr 2018 18:43:35 +0100 Received: from [195.171.43.32] (helo=relay1.thorcom.net) by post.thorcom.com with esmtp (Exim 4.14) id 1f5apL-0003Rc-AJ for rsgb_lf_group@blacksheep.org; Mon, 09 Apr 2018 18:43:35 +0100 Received: from resqmta-ch2-12v.sys.comcast.net ([69.252.207.44]) by relay1.thorcom.net with esmtps (TLSv1.2:ECDHE-RSA-AES256-GCM-SHA384:256) (Exim 4.89) (envelope-from ) id 1f5apG-000825-5x for rsgb_lf_group@blacksheep.org; Mon, 09 Apr 2018 18:43:34 +0100 Received: from resomta-ch2-02v.sys.comcast.net ([69.252.207.98]) by resqmta-ch2-12v.sys.comcast.net with ESMTP id 5amnfbDD53HAQ5an9fy7HS; Mon, 09 Apr 2018 17:41:19 +0000 X-DKIM-Result: Domain=comcast.net Result=Signature OK DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=comcast.net; s=q20161114; t=1523295679; bh=/fjOkGI7H3HKQCxmtjeAM8yFy9j6eHnjvSPHIAB8/H0=; h=Received:Received:Message-ID:From:To:Subject:Date:MIME-Version: Content-Type; b=chyGyYZivcaySjbyWYVpBAYnfJB+sUYuvEeXXLRalu5RSqEWWld3wxzfbPgtnXAS1 ubP0eV4wJhxkkECFCavQXmAo3uy87eYbqdf0owTWa6oZI0H45xhl0cy1oGfTFvuR9e jdKIVX+vNiMkewjgoYDCmfUlM5ryiwINn/q61rmLbu9Agvt6Pwx2F4TYjJNng/l8lD eaDH/HeuDFOxdLY8XFOkJortGW7LcLhPv0Fl5yXz60euEws3beS8lmxyixreCK4RA3 JYopdGbm5L0JBHLKJd/1IWBM/GD1hcwxCJ45RaPpXqmYzJa2BwWo0cUXNaPb1BqFXG HN+G2Ht4/XDsA== Received: from DELL4 ([73.4.253.141]) by resomta-ch2-02v.sys.comcast.net with SMTP id 5an6fms3etHiS5an7fzShd; Mon, 09 Apr 2018 17:41:19 +0000 Message-ID: <1539CCA16B9A4092972CB000BE4C440A@DELL4> From: To: References: <162a4797468-1db9-bdf2@webjas-vae168.srv.aolmail.net> <1UQROqZht1.1c1VdzC0S69@optiplex980-pc> <3a0c0669-018b-13a7-b56b-dd3f63fab464@n1bug.com> <197556217.20180409124931@gmail.com> <37574432-b72e-f2d1-0e85-af19dd970817@n1bug.com> <4D19B3707137430CBE04857FBA5C80B1@gnat> <1b882ae9-fede-3ec4-256e-9b068d3acf99@n1bug.com> Date: Mon, 9 Apr 2018 13:41:16 -0400 MIME-Version: 1.0 X-Priority: 3 X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook Express 6.00.2900.5512 X-MimeOLE: Produced By Microsoft MimeOLE V6.00.2900.5512 X-CMAE-Envelope: MS4wfHp7ZX+4dHWj92AULURZNKAvkKvNVJlAFQjymzbivw+dX9E9Mi4eKeBcrMwGK5UoGtZDF1AJYHRQSrXG0fs1PQMOqPRdTKbGf0YtQVdohsW2rDohKiLM nlx7GYSHh8RPNqSyK1/zF6n+FxIuZv4lFxfABMnMEkkjCai3ftY0uzSG X-Spam-Score: 1.0 (+) X-Spam-Report: Spam detection software, running on the system "relay1.thorcom.net", has NOT identified this incoming email as spam. The original message has been attached to this so you can view it or label similar future email. If you have any questions, see the administrator of that system for details. Content preview: Paul Thanks for the photos and information. I was more interested in the superimposed gate waveforms than the drains, though. A pix of the LPF as well would be appreciated ... think there was one last week. Just for the record ... my doubler was never mounted inside the amplifier ... so you are covering new ground with that. I would think having it external to the amplifier would be less problematic. For testing, stick to driving it with the HP3325A for now ... which is what you're most likely already doing. [...] Content analysis details: (1.0 points, 5.0 required) pts rule name description ---- ---------------------- -------------------------------------------------- 0.1 URIBL_SBL_A Contains URL's A record listed in the Spamhaus SBL blocklist [URIs: n1bug.com] 0.6 URIBL_SBL Contains an URL's NS IP listed in the Spamhaus SBL blocklist [URIs: n1bug.com] 0.2 STOX_REPLY_TYPE No description available. 0.0 FREEMAIL_FROM Sender email is commonly abused enduser mail provider (jrusgrove[at]comcast.net) 0.0 T_DKIM_INVALID DKIM-Signature header exists but is not valid X-Scan-Signature: ead411ce91f9601ce3974c7575797436 Subject: Re: LF: W1VD amp help - more waveforms Content-Type: text/plain; format=flowed; charset="UTF-8"; reply-type=original Content-Transfer-Encoding: 7bit X-Spam-Checker-Version: SpamAssassin 2.63 (2004-01-11) on post.thorcom.com X-Spam-Level: * X-Spam-Status: No, hits=1.9 required=5.0 tests=FORGED_MUA_OUTLOOK, NO_REAL_NAME autolearn=no version=2.63 X-SA-Exim-Scanned: Yes Sender: owner-rsgb_lf_group@blacksheep.org Precedence: bulk Reply-To: rsgb_lf_group@blacksheep.org X-Listname: rsgb_lf_group X-SA-Exim-Rcpt-To: rs_out_1@blacksheep.org X-SA-Exim-Scanned: No; SAEximRunCond expanded to false Paul Thanks for the photos and information. I was more interested in the superimposed gate waveforms than the drains, though. A pix of the LPF as well would be appreciated ... think there was one last week. Just for the record ... my doubler was never mounted inside the amplifier ... so you are covering new ground with that. I would think having it external to the amplifier would be less problematic. For testing, stick to driving it with the HP3325A for now ... which is what you're most likely already doing. Can't find much fault with the construction ... other than the somewhat loose primary winding on the transformer. In mine, the primary winding was nestled inbetween the turns of the secondary. This is important to minimize leakage reactance ... which also contributes to excessive ringing. Think I would continue to concentrate on getting the ringing down before going to high power. One other thing ... have you double checked that you have the correct capacitance in the LPF? Jay W1VD ----- Original Message ----- From: "N1BUG" To: Sent: Monday, April 09, 2018 11:34 AM Subject: Re: LF: W1VD amp help - more waveforms > Yep, voltage breakdown of the FETs was my worry. However I may be > making a false assumption. I assumed the voltage spikes in the > ringing would vary linearly with applied drain voltage? Perhaps that > isn't necessarily so? > > With 13V on the drains the first spike here is 'about' 64V. > > Efficiency seems fine. I wouldn't try to put an exact figure to it > what with measurement accuracy in three places (voltage, current, RF > power) but it 'appears' to be in the mid 90s. > > Paul > > > On 04/09/2018 11:02 AM, jrusgrove@comcast.net wrote: >> Alan >> >> The main concern about the ringing is that the positive extreme stays below the drain source >> breakdown voltage ... with some 'headroom'. Otherwise ... >> >> Jay W1VD >> >> >> ----- Original Message ----- >> From: "Alan Melia" >> To: >> Sent: Monday, April 09, 2018 10:21 AM >> Subject: Re: LF: W1VD amp help - more waveforms >> >> >>> Paul >>> I think you need to step back from this a little. One point, design/cable routing at 137kHz is >>> normally not that critical and it is unlikely it is having much effect. Many us have >>> ''haywired'' >>> PAs at these frequencies without major troubles....even using croc-leads!! >>> >>> You are unhappy about the drain waveforms.......why?? the ringing is on the ''off'' device and >>> so >>> doesnt really matter in terms of efficiency. Consider what is happening. The FET drive goes off >>> and the drain current starts to drop inductance in the drain feed causes the voltage to rise to >>> try to keep the current flowing. Then on top of this the other transistor switches on and the >>> transformer connection for the off side sees a rising induced voltage out of the transformer. >>> There is bound to be overshoot but it does not absorb much power. It may be the generous ''dead >>> zone'' (whilst a good idea) that is producing this picture. >>> >>> The critical part is the the flat zero volt line when the FET is on. The current pulse rings a >>> bit, but the current drops in the second half of the pulse.....why?? This, I think, is really >>> the >>> loss of power. Does Jay's show this? The point I am making is don't get drawn up blind alleys >>> because a trace just does not look ''pretty''. >>> >>> I think we have mentioned this before but the transient performance of the power supply may be a >>> factor. There should not be great changes in the current draw because you are switching the PSU >>> load from one transistor to the other but there can be higher speed transients that can affect >>> power supply regulators in unexpected ways. >>> >>> As Andy said efficiency at 12v is not very meaningful because of the high rds of these FETs. It >>> is >>> usefull to run up a PA at low volts say for safety when the antenna needs to be tuned. >>> >>> Finally the scope probes are placing an. albeit small, capacitance across the drains (I am >>> assuming they are correctly trimmed) The waveform can often be affected by where the ground is >>> picked up from. >>> >>> Stick with it because you are close to being ''there'' >>> >>> Alan >>> G3NYK >