Envelope-to: dave@picks.force9.co.uk Delivery-date: Mon, 23 May 2005 17:45:10 +0100 Received: by ptb-mxcore04.plus.net with spam-scanned (PlusNet MXCore v2.00) id 1DaG3B-0003T9-Kv for dave@picks.force9.co.uk; Mon, 23 May 2005 17:45:10 +0100 Received: from post.thorcom.com ([193.82.116.20]) by ptb-mxcore04.plus.net with esmtp (PlusNet MXCore v2.00) id 1DaG3B-0003Sn-7W for dave@picks.force9.co.uk; Mon, 23 May 2005 17:45:09 +0100 Received: from majordom by post.thorcom.com with local (Exim 4.14) id 1DaG2q-0003FY-5y for rs_out_1@blacksheep.org; Mon, 23 May 2005 17:44:48 +0100 Received: from [193.82.116.30] (helo=relay.thorcom.net) by post.thorcom.com with esmtp (Exim 4.14) id 1DaG2p-0003FP-JK for rsgb_lf_group@blacksheep.org; Mon, 23 May 2005 17:44:47 +0100 Received: from hestia.herts.ac.uk ([147.197.200.9]) by relay.thorcom.net with esmtp (Exim 4.43) id 1DaG2o-0001q8-Ux for rsgb_lf_group@blacksheep.org; Mon, 23 May 2005 17:44:47 +0100 Received: from altair ([147.197.215.111] helo=altair.herts.ac.uk) by hestia.herts.ac.uk with esmtp (Exim 3.22 #1) id 1DaFpX-0003tH-00 for rsgb_lf_group@blacksheep.org; Mon, 23 May 2005 17:31:03 +0100 Received: from [147.197.164.230] (helo=RD40002) by altair.herts.ac.uk with esmtp (Exim 4.42) id 1DaFpX-0003lz-4v for rsgb_lf_group@blacksheep.org; Mon, 23 May 2005 17:31:03 +0100 From: "james moritz" To: rsgb_lf_group@blacksheep.org Date: Mon, 23 May 2005 17:31:03 +0100 Message-ID: <000001c55fb4$cf915f50$e6a4c593@RD40002> MIME-Version: 1.0 X-Priority: 3 (Normal) X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook, Build 10.0.4510 Importance: Normal In-Reply-To: X-MimeOLE: Produced By Microsoft MimeOLE V6.00.2900.2180 X-UH-MailScanner: No Virus detected X-UH-MailScanner-From: j.r.moritz@herts.ac.uk X-SPF-Result: relay.thorcom.net: 147.197.200.9 is neither permitted nor denied by domain of herts.ac.uk Subject: LF: RE: Loop antenna problem Content-Type: text/html; charset=windows-1252 X-SA-Exim-Scanned: Yes Sender: owner-rsgb_lf_group@blacksheep.org Precedence: bulk Reply-To: rsgb_lf_group@blacksheep.org X-Listname: rsgb_lf_group X-SA-Exim-Rcpt-To: rs_out_1@blacksheep.org X-SA-Exim-Scanned: No; SAEximRunCond expanded to false X-PN-SpamFiltered: by PlusNet MXCore (v2.00) Content-transfer-encoding: 8bit

Dear J.B., LF Group,

 

I think the problem here is the size of the coupling loop, which is only slightly smaller diameter than the main loop, is too large. If the coupling loop had unity coupling factor to the main loop, the complete loop would be a 15:1 transformer. If the RX Zin is 50R, the transformed load across the main loop terminals would be 50 x 15^2 = 11.2k. With a loop inductance around 2.1mH, the loaded Q is then only about 6 or so. In fact, the loading will be reduced by the less-than-unity coupling factor between the main loop and the coupling loop; this is difficult to calculate due to all the variables involved, but a rough guess would be an overall impedance ratio of about 450:1, making the shunt resistance about 22k, and the loaded Q of the loop around 12, still very low. Going further with the rough calculations, 1uV/m field strength would then only give you about 0.2uV at the RX input at best. This comes out similar to an un-tuned 40m delta-loop, which ought to have about 80m^2 area. So that is reasonably consistent with what you are observing.

 

With an unloaded Q of 380, the shunt resistance across the loop terminals should be about 680k. Matching this to the RX input (to achieve maximum signal level) requires an impedance transformation ratio of about 14000:1. The loaded Q of the loop would then be 190, and the voltage at the RX for 1uV/m signal ought to be around 0.6uV, so about 9 or 10dB improvement, plus much sharper selectivity. If the unloaded Q of the loop is lower, the output will also be slightly lower, and the optimum impedance transformation ratio lower too. The way to get these higher impedance transformation ratios is to make the coupling loop smaller, I would guess somewhere around 1 - 1.5m in diameter would be about right. As the others have said, I don’t think screening and balancing the coupling loop will make a significant practical difference, so a plain bit of wire would be as good as anything, and easy to play around with to get the optimum size.

 

The other suggestions of using a capacitive tap, or a series transformer, should also work well – I would estimate a capacitor of around 50 – 70nF would be right, or a series matching transformer with a 1:2 or 1:3 step up ratio feeding the 50 ohm cable.

 

Cheers, Jim Moritz

73 de M0BMU

 

-----Original Message-----
From: owner-rsgb_lf_group@blacksheep.org [mailto:owner-rsgb_lf_group@blacksheep.org] On Behalf Of J. B. Weazle McCreath
Sent: 21 May 2005 00:52
To: rsgb_lf_group@blacksheep.org
Subject: LF: Loop antenna problem

 

Hello LF Group,

 

I've finally finished the construction of my LF loop and I appear to have a

problem with it regarding the connection to the receiver.  The loop itself

is in the form of an octagon, with an overall diameter of 10.5 feet, and it

consists of 15 turns of number 12 THHN stranded wire.  The spacing of

the turns is 0.25 inch and the tuning is done with a 3 gang, 400 pF. per

section, variable capacitor with all sections connected in parallel….

 

The problem is with the pickup loop, which is of the classical shielded

construction as described in many antenna books.  Mine is made from

RG-213 coax and it's positioned roughly six inches inside of the main

loop windings, but in the same plane 

 

73, J.B. Weazle McCreath, VE3EAR - VE3WZL