Return-Path: Received: (qmail 20276 invoked from network); 5 Aug 2001 20:51:48 -0000 Received: from unknown (HELO murphys-inbound.services.quay.plus.net) (212.159.14.225) by excalibur-qfe1-smtp-plusnet.harl.plus.net with SMTP; 5 Aug 2001 20:51:48 -0000 Received: (qmail 28896 invoked from network); 5 Aug 2001 20:51:35 -0000 Received: from unknown (HELO post.thorcom.com) (212.172.148.70) by murphys with SMTP; 5 Aug 2001 20:51:35 -0000 Received: from majordom by post.thorcom.com with local (Exim 3.16 #2) id 15TUnc-00044O-00 for rsgb_lf_group-outgoing@blacksheep.org; Sun, 05 Aug 2001 21:47:00 +0100 Received: from fep01.swip.net ([130.244.199.129] helo=fep01-svc.swip.net) by post.thorcom.com with esmtp (Exim 3.16 #2) id 15TUnb-00044J-00 for rsgb_lf_group@blacksheep.org; Sun, 05 Aug 2001 21:46:59 +0100 Received: from oemcomputer ([212.151.108.145]) by fep01-svc.swip.net with SMTP id <20010805204618.FWQE18391.fep01-svc.swip.net@oemcomputer> for ; Sun, 5 Aug 2001 22:46:18 +0200 Message-ID: <001201c11de7$6051a9a0$916c97d4@oemcomputer> From: "Johan Bodin" To: rsgb_lf_group@blacksheep.org Subject: SV: LF: Harmonic sampling (Was: Decimation) Date: Sun, 5 Aug 2001 22:46:14 +0300 MIME-Version: 1.0 Content-Type: text/plain; charset=iso-8859-1; format=flowed Content-Transfer-Encoding: 8bit X-Priority: 3 X-MSMail-Priority: Normal X-Mailer: Microsoft Outlook Express 4.72.3110.5 X-MimeOLE: Produced By Microsoft MimeOLE V6.00.2800.1106 Precedence: bulk Reply-To: rsgb_lf_group@blacksheep.org X-Listname: rsgb_lf_group Sender: Paul, >An undersampling system needs some kind of sample & hold circuit. IIRC from >digital audio, the aperture time should be less than T/10 (T=sampling >period) in order to keep the high frequency rolloff below 1 dB. Yes, the figures sounds reasonable. >So if we assume a hypothetical 300 kHz sampling rate (for 0 .. 140 kHz BW), >the aquisition time should be less than 300 ns, which should not be too hard to >implement:-). Since the hold time is about 170 us (6 kHz), we are talking >about 1:500 aquisition/hold time ratios, which can be a problem due to hold >time leakage. Yes, the 1:500 ratio could turn the S/H "droop rate" into a problem. I was thinking about using a cheap 74HC4066 or similar analog switch as sampling gate but after giving it a second thought I realised that it is probably out of the question due to the high "charge injection" from the control pin to the switch i/o pins. The hold cap' has to be quite small in order to meet the acquisition time requirement so the control pulse leakage will probably upset things... Assuming S/H driver source resistance + switch R-on = 50 ohms, C has to be about 10nF for -3dB at 300kHz but... At an aquisition/hold time ratio of 1:500, C must be <= 20pF. Among other things, this calls for a buffer amplifier having almost zero bias current :~) Do you have any suggestion for a hombrew S/H circuit? Diode ring gate? Ready made S/H chip? I have no experience of building fast S/H circuits. >By adding dithering noise, low and medium frequency tones could be reproduced >well below -100 dB, when the teoretical limit for a 16 bit system would be -96 dB. Yes, isn't it funny...The system performance can sometimes be improved by ADDING noise! The dithering noise spectrum has to be outside the wanted passband of course. >If some super-selective front end is used (say 250 Hz bandwidth) in the LF >receiver, the digital signal may contain signal related quantisation noise, >thus some form of dither noise may be required. However, if the analog >bandwidth is larger, I guess that the band noise may be used as dither noise. Yes. Steve VK2ZTO did some extreme narrowband experiments on longwave using a 1-bit ADC. I think it was a simple comparator hooked on the RX audio output. Dithered by natural band noise, the signal appeared to have many bits of resolution after the decimation. Fs=6kHz seems like a good choice. The selected Fs harmonic should be just outside the band of interest (lowest acceptable beat note) and the preselector BW (-many dB!) must be less than Fs/2. Pse correct me if I'm wrong. >>From this description, it appears as if this device is actually a 13 bit >flash ADC and the three extra bits are generated by the Fs/8 downsampling >:-). Right. It's not a true 16-bit ADC. It is some kind of combination of a sigma-delta with 5-bit flash & 5-bit feedback and a 12-bit pipelined ADC. Some data: - Fs <= 20MHz - 1 MHz signal BW - SNR 89 dB - THD -98dB - SFDR 100dB - Equiv. input noise 0.6 LSB - Stopband attenuation 85 dB Unfortunately, my preliminary data sheet doesn't tell the ENOB (effective number of bits). I actually have two of these chips and a HSP50016 DDC too. I hope that I someday will find some time to play with them... Anyway, the harmonic sampling idea is *very* appealing. 73 Johan SM6LKM